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농용(農用) 내연기관(內燃機關) 폐열(廢熱)의 열(熱)에너지 회수(回收)(I) -시스템 설계(設計)와 주변수(主變數) 분석(分析) 및 실험(實驗)-
서상룡,유수남,Suh, S.R.,Yoo, S.N. 한국농업기계학회 1986 바이오시스템공학 Vol.11 No.2
A waste heat recovery system for an internal combustion engine for agriculture was developed. The system is for recovering both of exhaust heat and cooling heat of an engine and is so simple in its structure that can be used in rural area easily. A series of experiment was carried out to the experiment which will be discussed later on, collect data for the performance of the system at various operating conditions of the system and an engine and to determine a range of coolant temperature in which performance of an engine is not affected by the heat recovery system incorporated. The obtained experimental data is not only useful to materialize performance of the system at the experimental conditions but also to construct a mathematical model of the system to predict the system variables beyond the scope of
농용(農用) 내연기관(內燃機關) 폐열(廢熱)의 열(熱)에너지 회수(回收)(II) -시스템 Simulation과 안정성(安定性) 실험(實驗)-
서상룡,유수남,Suh, S.R.,Yoo, S.N. 한국농업기계학회 1987 바이오시스템공학 Vol.12 No.1
A mathematical model for the waste heat recovery system for an engine was developed. The model based on the experimental data reported before was validated and was used to predict the waste heat recovery and recoverable heat of the engine at various operating conditions of the engine and the system. The model was also used to determine flow rates of the circulating water in the system for a certain temperature increment of the water at various operating conditions of the engine to give basic data to design the system. Stability of the system performance was tested on subjects of vapor lock problem, thermal characteristics of the thermostatic valve, and temperature variation of the circulating water in the engine and fuel consumption of the engine during each mode of the system operation and its change into the other. The test showed that the system operation was stable enough. Temperature profile in the thermal energy storage (TES) was observed during storing thermal energy, and thermal stratification in the TES was well formed acceptable to be used in the system. Finally a scheme to automatize the system was suggested.
서상룡,최재갑 한국농공학회 1975 한국농공학회논문집 Vol.17 No.4
This study was carried out to develop a method of grain drying ststem that can be done by forcing the heated-air directly into the grains within the sack. The air duct was pushed into the central position of the grain-deposited sack and the heated-air was forced to flow in the radial direction. The system is referred here as the unit sack drying system. At a first step of this study, an air flow resistance tester was constructed to measure the resistance of air flow to grains in cooperated with some different sack materials, the sack materials, the tested were rice-straw bag, sack of polyethylene film, and jute sack In addition, unit sack drying system was constructed to investigate the drying characteristics of the dryer. on this dryer, two kind of terminal air ducts were attached and tested to examine its effects on uniform drying, and also, aseries of drying test was performed to trace the effect of increasing air flow rate on uniform drying. The results are as follows: 1) Resistance of air flow for each sack material was increased almost proportional to the increasing rate of air flow. Experimental data showed little significant differences of the air flow resistance among the materials. 2) From the comparison with air flow resistance of sack material and that of roughrice, it was indicated that airflow resistance of sack material was much higher than that of rice rough Therefore, in the unit sack drying sysle in which air flow is destined to face the sach material after leaving the grain, it was suggested that air flow would be inuniform to each part of grain within sack because of much higher air flow resistance of sack material than that of grain, and the fact would results inuniform grain drying. 3) Drying test on the unit sack drying system in cooperated with different type of terminal air ducts showed that high speed air is better for uniform drying than in high pressure. with the drying system which was assembled with the air ducts delivering higher speed air, there also involved a problem of significant inuniform drying. Therefore, any means to improve the inuniform drying should be undertaken for practical use. 4) A series of drying test with in creasing air flow rate resulted that increasing air flow rate in the unitsack drying system gave little effect on uniform drying, therefore, it is recommened to change its drying system for drying grain uniformly.