http://chineseinput.net/에서 pinyin(병음)방식으로 중국어를 변환할 수 있습니다.
변환된 중국어를 복사하여 사용하시면 됩니다.
외부하중을 받는 선형 롤러베어링의 LM 블록 변형을 고려한 변위 모델링
권선웅(Sun-Woong Kwon),통반칸(Van-Canh Tong),홍성욱(Seong-Wook Hong) 대한기계학회 2016 大韓機械學會論文集A Vol.40 No.12
선형 롤러베어링은 하중이 크고 정밀성이 요구되는 이송장치를 지지하기 위해 광범위하게 사용되는 기계요소이다. 본 논문에서는 외력을 받는 선형 롤러베어링의 변위를 계산하기 위한 새로운 모델링 방법을 제시하였다. 먼저 LM 블록을 강체로 가정하여 롤러와 LM 블록의 지배방정식을 유도하였고 Newton-Raphson법을 이용해 계산하였다. 롤러와 레이스 사이의 접촉하중은 롤러의 형상을 고려하여 슬라이싱 기법을 이용하여 계산하였다. 강체 LM 블록 모델에 의해 계산된 접촉하중을 활용하여 LM 블록의 구조적 변형을 유한요소 모델로부터 계산하였다. 최종적인 변위는 강체 LM 블록을 가정한 모델로부터 계산된 변위와 LM 블록 구조해석 결과를 조합하여 도출하였다. 제안된 방법에 의한 결과와 베어링 제작 업체 프로그램 결과와의 비교를 통해 제안된 방법을 검증하였다. Linear roller bearing (LRB) is an important mechanical element that is widely used in precise positioning systems that are subjected to large loads. This paper presents a new model for estimating the displacement of an LRB subjected to external forces. For this purpose, assuming that the linear motion block (LM block) is rigid, the equilibrium conditions for the LRB were obtained by solving the equilibrium equations of the rollers and the rigid LM block using the iterative Newton-Raphson method. The contact loads between the rollers and raceways were determined considering the profiled rollers. Then, the structural deformations of the LM block, subjected to the contact loads from the rigid LM block model, were computed using a finite element model for the LM block. The displacements of the LRB were then determined by superposition of the rigid LM block displacements on the induced displacements due to the structural deformations of the LM block. The proposed method was verified through comparison with a program by the bearing manufacturer.
서인석(In Seok Seo),김병군(Byung Goon Kim),박승국(Seung Kook Park),권선웅(Sun Woong Kwon) 한국물환경학회 2000 한국물환경학회지 Vol.16 No.4
Intermittently aerated activated sludge process was applied as a water reuse process of 70 ㎥ /day for the upgrade of organic, nitrogen and phosphorus removal efficiency and clarifier performance. After application of the intermittently aeration, removal efficiency of BOD, SS, T-N and T-P were achieved 95%, 90%, 80% and 60%, respectively. Removal efficiencies in intermittently aerated process were considerably increased, comparing to those of continuously aerated activated sludge process. Also sludge rising problem in clarifier was improved. Average concentration of supplied reusing water were BOD 5 ㎎/L, turbidity 4 NTU and after chlorination, residual chlorine 0.4 ㎎/L, coliform 0 MPN/100mL. Intermittently aerated activated sludge process could be one of the best alternative process for the retrofit of conventional activated sludge process for the removal of nutrient in water reuse system.