http://chineseinput.net/에서 pinyin(병음)방식으로 중국어를 변환할 수 있습니다.
변환된 중국어를 복사하여 사용하시면 됩니다.
박홍석(Hongseok Park),박성범(Sungbum Park),문상민(Sangmin Moon),이창우(Changwoo Lee),이규봉(Gyubong Lee) 한국자동차공학회 2005 한국자동차공학회 춘 추계 학술대회 논문집 Vol.2005 No.5_2
Nowadays, the automation in assembly field with robot gets an increasing importance. The putting of spare tire in trunk is still dominated by free dropping. By that parts in trunk, e.g. luggage room lamp, jack and so on were damaged and the complaint of assembler in the next process was occurred due to physical strength. To eliminate these, the robot system was in this paper developed to place spare tire on the mounting hole in trunk. The movement of robot was synchronized with the velocity of chassis hanger.<br/> With this automated system the productivity of the assembly line was increased from the benefits such as simplification of the system using only robot without the mechanically synchronized transport, inserting spare tire into the right position with robot, reduction of damaged parts and production of various type of car.