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        Experimental and numerical investigation on a novel gas turbocharging system for diesel engine power recovery at high altitude

        Dengfeng Yang,Li’ang Cao,Yang Liu,Zhilian Zhang 대한기계학회 2019 JOURNAL OF MECHANICAL SCIENCE AND TECHNOLOGY Vol.33 No.10

        Based on the analysis of the plateau performance for a 6 cylinder 8.6 L turbocharged diesel engine, a novel gas turbocharging system (GTS) is proposed to recover the engine power at high altitudes. Besides, a rolling-reflux combustor is designed to meet the structural requirements of GTS as well as to reduce the flow loss. Both the structure of the rolling-reflux combustor and the cycle thermal calculation of the GTS were described in detail in present work. The performance changes and the fuel consumption rate with engine speed at different altitudes of the GTS are compared to the original engine. Results show that when the altitude changes from 3 km to 5 km, the torque and power of the diesel engine with GTS can be recovered to that at sea level. Then, the particle image velocimetry (PIV) test is performed to study the cold flow field at the cylinder head of the rolling-reflux combustor, and the flow conditions are analyzed in detail. Finally, the flow bench is built and the aerodynamic experiment is carried out to verify the effectiveness of GTS.

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        Investigations on the effect of guide vane thickness and solidity on shock and unsteady flow characteristic of VNT

        Dengfeng Yang,Li’ang Cao,Ce Yang,Dazhong Lao,Harold Sun 대한기계학회 2020 JOURNAL OF MECHANICAL SCIENCE AND TECHNOLOGY Vol.34 No.6

        In this work, the influence of thickness and solidity of guide vane on the unsteady flow of a radial inflow turbine with variable nozzle has been numerically studied. Three vanes with the thickness changes from 0.3 to 0.1 and the solidity changes from 1.43 to 2.86, were chosen for this study. By investigating the unsteady flow field, it is found that the vane with low thickness and high solidity (vane B) can reduce shock by 75 % compared to the vane with high thickness and low solidity (base model); meanwhile, it can also mitigate the nozzle endwall leakage flow thus improves the flow uniformity of rotor inlet. As the intensity of shock and nozzle leakage flow were mitigated, the aerodynamic loading fluctuation of rotor blade can be weakened effectively, which will lead to improved rotor blades forced response. However, at small opening, vane B shows about 0.5 % lower efficiency than the base model; at large open condition, the efficiency degradation of vane B is up to 1.4 %. Therefore, there is a trade-off between the efficiency and forced response when choosing the nozzle vane solidity and thickness.

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